The Engine and transmission
is now installed along with the radiator and hoses etc. The distributor
and generator only required stripping cleaning and re assembly. The heat
insulation seen fitted to the left hand foot well is cement sheet with
a foil layer underneath instead of the original asbestos. The two strips
seen below originally only covered the foot well from the inner edge to
the brace.
I think I have the wiring layout
right (thanks Ward), but would be happy to hear from anyone who disagrees
on any aspect of the engine bay layout. I'm still getting round to making
the brass eye used to attach the copper oil line to the firewall and the
cable bracket for the cold air intake. I have deliberately taken the wiring
for the flasher unit inside the cabin, rather than mounting it in the engine
bay, as a result of suggestions that is is easier to hear the tick which
reminds the driver that they are on. The two wires for this can be seen
at the extreme right of the image below.
One of the exhaust manifold
outlet flange studs, which at some point had at some point been re tapped
(at an angle) had to be plugged and re tapped square. The carburetors are
from an old Austin as they were not supplied with the car. I sent
the carburetor bodies to Midel in Sydney for re bushing and they were able
to supply me with all of the components I needed from stock to refurbish
them, including the correct choke arms. The copper line between the carburetor
float bowls I fabricated myself. I'm not sure that I have the throttle
linkages original, but this layout provides a long pedal travel and at
rest, the pedal is level with the brake pedal.
The gearbox had unfortunately
been stored without any oil in it since the 50's. A build up of condensation
in the housing had caused surface rust on the bearings and jammed the shift
cross shaft in the side plate. A new cross shaft was machined, hardened
and ground and the input shaft and main shaft bearings replaced. Otherwise
the condition of the gearbox was excellent. The gearbox rear mounts which
are incorporated into the Laycock overdrive unit, had been broken off when
the car was crashed and welded back on. The heat from welding caused significant
distortion in the housing that wasn't picked up at the time. The housing
has now been re machined to correct this problem.
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